Show simple item record

dc.contributor.authorQuezada, Erick
dc.contributor.authorPretel, Lisbeth
dc.contributor.authorSantamaría, Carla
dc.contributor.authorValencia, Nathaly
dc.contributor.authorYépez, Amanda
dc.contributor.authorCubas, Julio
dc.date.accessioned2021-08-17T03:07:59Z
dc.date.accessioned2022-02-22T12:17:14Z
dc.date.available2021-08-17T03:07:59Z
dc.date.available2022-02-22T12:17:14Z
dc.date.issued2021-07
dc.identifier.isbn978-958-52071-8-9
dc.identifier.issn2414-6390
dc.identifier.otherhttp://laccei.org/LACCEI2021-VirtualEdition/meta/FP57.html
dc.identifier.urihttp://dx.doi.org/10.18687/LACCEI2021.1.1.57
dc.identifier.urihttp://axces.info/handle/10.18687/20210101_57
dc.description.abstractAbstract– The purpose of this study is to implement preventive maintenance in the company Pesquera Pacasmayo E.I.R.L. This study arises after identifying the constant problems in the production area among those that stand out in the maintenance area. The study has a pre-experimental design in which a series of data collection techniques and instruments were used, specifically in the analysis of information on the company's production and maintenance processes. It begins by making a diagnosis of these areas to identify the problems that directly affect productivity in order to determine the maintenance tools to apply; We proceed to find the Average Time between Failures considering the real-time work data and the number of failures, finding the value of 40 hours for the main machine, 70.94 hours for the Hydraulic Generator, and 54.36 hours for the Refrigeration Compressor, Average time between repairs considering the data of the stoppage time due to breakdown and the number of breakdowns, finding the value of 5 hours for the main machine, 3.5 hours for the Hydraulic Generator, and 4 hours for the Refrigeration Compressor, and the availability concluding that there is an availability of 89% for the main machine, 95% for Hydraulic Generators and 93% for Refrigeration Compressors. Preventive maintenance was applied to minimize these problems, in addition to this, tools such as TPM were also applied. This is reflected in an increase in productivity, as well as an increase in total Team Effectiveness to 15%.en_US
dc.language.isoEnglishen_US
dc.publisherLACCEI Inc.en_US
dc.rightsLACCEI License
dc.rights.urihttps://laccei.org/blog/copyright-laccei-papers/
dc.subjectMTBFen_US
dc.subjectMTTRen_US
dc.subjectAvailabilityen_US
dc.subjectPreventive Maintenanceen_US
dc.subjectTPM.en_US
dc.titleDesign proposal of a Maintenance Management System for the Company Pesquera Pacasmayo E.I.R.L.
dc.typeArticleen_US
dc.description.countryPeruen
dc.description.institutionUniversidad Privada del Norte (UPN)en
dc.description.trackEngineering Design, Engineering Materials and Engineering Innovationen
dc.journal.referatopeerReview


Files in this item

Thumbnail

This item appears in the following Collection(s)

  • 2021 LACCEI - Virtual Edition
    The Nineteenth LACCEI International Multi-Conference for Engineering, Education Caribbean Conference for Engineering and Technology.

Show simple item record